Thank you for the replies. That jig would have come in very handy.
After another dozen attempts I finally managed to get the TS75 calibrated to the TS55 REQ. I ended up having to adjust the TS55REQ in towards the rail 1st. I pushed the body / blade all the way towards the rail so the was no more adjustment. Made a reference cut, it was very toed in at this point, but the cut was actually pretty decent. Using feeler gages I set the front of the blade at .010 inches and the back at .016 inches.
View attachment 1
Tightened eveything back up double checking the blade location. Moved the rail over and made a new reference cut. Set the TS75 on the rail and set the blade so it was touching at the front and .006 clearance at the back.
Made a cut with the TS75 with the rail at the same location, and...
View attachment 2
So something moved, this happened several times and seemed to be pretty consantant. I would set the front of the blade so it was just kissing the material of the reference cut and then when I would do a cut it would remove an addition .020.
So using that I set the front of the blade at .016 and the back at .022 and finally got very close that I could see the TS55REQ was not quite at 90 degrees.
View attachment 3
Reset the TS55REQ at 90 degrees and made a new cut. Then made a cut with the TS75 and they both cut at the same place on the rail. Luckily since everything moved in all my rails won't need new splinter guard strips.
A tedious process but I am glad its done.